My '75 F150 with 360 2100 motorcraft carb warner 4 speed and AC/PS
was getting too hot too...
I had a leak in my vacuum advance motor, replaced.
Installed a -new- water pump and cap checked for good seal there.
Replaced my leaky after market (added it myself) clutch fan clutch.
Experimented with some main jet changes went back to what I had.
My over heating went away right after I did the next thing tho...
Went from a three core to a four core radiator that was about $307.
The old radiator was in good shape but dirty (only on the outside)
from weeping, of course any leaks, even slight, have a real negative
effect.
If I had an automatic I would consider an extra raditor for it
instead of adding that heat to my engine. But don't know nuthing
about it really. :/
Anyway... my setup never held the amount of water and coolant that
the service manual sez it should... until I replaced the original
designed radiator with that new four core...now it's right on the
money- what they said it should be. Ford shorted me on a simple
radiator, no kidding. :/
Here lately it's running even cooler after I cut into the exhaust Y
pipe and found it really crappy looking in there. It looked like a
football shaped torch cut hole with lots of slag hanging from it and
the hole was no bigger than a golf ball!

Ford shorted me there
too. Hey, it has more power now that -both- sides of the engine are
running.
Alvin in AZ